News 4 has obtained copies of two complaints filed in Federal …
Updated: Wednesday, 25 Mar 2009, 5:50 PM EDT
Published : Wednesday, 25 Mar 2009, 11:44 AM EDT
WASHINGTON (AP) - Federal safety investigators say the flight data recorder from
last month's air crash near Buffalo, N.Y., doesn't reveal the plane
had icing problems immediately before the crash. All 49 people
aboard the plane and one man in the house died.
The National Transportation Safety Board said Wednesday it is
continuing to examine the Q400 Bombardier's deicing system and
probe the flight crew's training.
Continental Connection Flight 3407 was about five miles short
of the Buffalo Niagara International Airport flying in icing
conditions the night of Feb. 12 when the plane tumbled wildly out
of control and plummeted onto a house.
Copyright 2009 The Associated Press.
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Update from NTSB below:
In its continuing investigation into the crash of Colgan Air
Flight 3407 in Clarence Center, New York, the National
Transportation Safety Board has released the following factual
information.On February 12, 2009, about 10:17 p.m. Eastern Standard
Time (EST), a Colgan Air Inc., Bombardier Dash 8-Q400, N200WQ,
d.b.a. Continental Connection flight 3407, crashed during an
instrument approach to runway 23 at the Buffalo-Niagara
International Airport (BUF), Buffalo, New York.
The crash site was approximately 5 nautical miles northeast
of the airport in Clarence Center, New York, and mostly confined to
one residential house. The 4 crew members and 45 passengers
were fatally injured and the airplane was destroyed by impact
forces and post crash fire. There was one ground
fatality. Night visual meteorological conditions prevailed at
the time of the accident.
The flight was a Code of Federal Regulations (CFR) Part 121
scheduled passenger flight from Liberty International Airport
(EWR), Newark, New Jersey to Buffalo.The NTSB has voted to conduct
a public hearing on this accident. The hearing, which will be
held May 12 - 14, 2009, at the NTSB's Board Room and Conference
Center in Washington, D.C., will cover a wide range of safety
issues including: icing effect on the airplane's performance,
cold weather operations, sterile cockpit rules, crew experience,
fatigue management, and stall recovery training.
The public hearing is part of the Safety Board's efforts to
develop all appropriate facts for the investigation. "The
tragedy of flight 3407 is the deadliest transportation accident in
the United States in more than 7 years," Acting Chairman Mark V.
Rosenker, who will chair the hearing, said. "The
circumstances of the crash have raised several issues that go well
beyond the widely discussed matter of airframe icing, and we will
explore these issues in our investigative fact-finding hearing."The
hearing will be held "en banc," meaning that all Members of the
NTSB will sit on the Board of Inquiry. Parties that will
participate in the hearing will be announced at a later time.The
aircraft wreckage has been moved from the accident site to a secure
location for follow-on inspections as may be needed.
A preliminary examination of the airplane systems has
revealed no indication of pre-impact system failures or
anomalies. Investigators will perform additional examinations
on the dual distribution valves installed in the airplane's de-ice
system. The de-ice system removes ice accumulation from the
leading edges of the wings, horizontal tail, and vertical tail
through the use of pneumatic boots. The dual distribution
valves, which transfer air between the main bleed air distribution
ducts and the pneumatic boots, were removed from the airplane for
the examination.
The airplane maintenance records have been reviewed and no
significant findings have been identified at this time.The ATC
group has completed a review of recordings of controller
communications with the flight crew during the accident flight and
conducted interviews with air traffic controllers on duty at the
time of the accident. The group has no further work planned
at this time.
Further review of the weather conditions on the night of the
accident revealed the presence of variable periods of snow and
light to moderate icing during the accident airplane's approach to
the Buffalo airport. Examination of the FDR data and
preliminary evaluation of airplane performance models shows that
some ice accumulation was likely present on the airplane prior to
the initial upset event, but that the airplane continued to respond
as expected to flight control inputs throughout the accident
flight. The FDR data also shows that the stall warning and
protection system, which includes the stick shaker and stick
pusher, activated at an airspeed and angle-of-attack (AOA)
consistent with that expected for normal operations when the de-ice
protection system is active.
The airplane's stick shaker will normally activate several
knots above the actual airplane stall speed in order to provide the
flight crew with a sufficient safety margin and time to initiate
stall recovery procedures. As a result of ice accumulation on
the airframe, an airplane's stall airspeed increases. To
account for this potential increase in stall speed in icing
conditions, the Dash 8-Q400's stall warning system activates at a
higher airspeed than normal when the de-ice system is active
in-flight to provide the flight crew with adequate stall warning if
ice accumulation is present.Preliminary airplane performance
modeling and simulation efforts indicate that icing had a minimal
impact on the stall speed of the airplane. The FDR data
indicates that the stick shaker activated at 130 knots, which is
consistent with the de-ice system being engaged.
FDR data further indicate that when the stick shaker
activated, there was a 25-pound pull force on the control column,
followed by an up elevator deflection and increase in pitch, angle
of attack, and Gs. The data indicate a likely separation of
the airflow over the wing and ensuing roll two seconds after the
stick shaker activated while the aircraft was slowing through 125
knots and while at a flight load of 1.42 Gs.
The predicted stall speed at a load factor of 1 G would be
about 105 knots. Airplane performance work is continuing.
Since returning from on-scene, the Operations & Human
Performance group has conducted additional interviews with flight
crew members who had recently flown with and/or provided
instruction to the accident crew, as well as personnel at Colgan
Air responsible for providing training of flight crews and
overseeing the management and safety operations at the
airline.
The group also conducted interviews with FAA personnel
responsible for oversight of the Colgan certificate, which included
the Principal Operations Inspector (POI) and aircrew program
manager for the Dash 8 Q-400.
The team has also continued its review of documentation,
manuals, and other guidance pertaining to the operation of the Dash
8 Q-400 and training materials provided to the Colgan Air flight
crews.The Operations & Human Performance group continues to
investigate and review documentation associated with the flight
crew's flight training history and professional development during
their employment at Colgan as well as prior to joining the
company.Post-accident toxicological testing of the flight crew was
performed by the FAA Civil Aerospace Medical Institute (CAMI)
toxicology lab.
Specimens taken from the first officer were negative for
alcohol, illicit substances, and a wide range of prescription and
over the counter medications. Specimens taken from the
captain were negative for alcohol and illicit substances, and
positive for diltiazem, a prescription blood pressure medication
that had been reported to and approved for his use by the Federal
Aviation Administration.The Safety Board is also examining several
other areas potentially related to the accident,
including: The circumstances of a recent event
involving a Dash 8-Q400, operated by Colgan Air, in which the
airplane's stick shaker activated during approach to the Burlington
International Airport (BTV) in Burlington, Vermont. A
preliminary review of the FDR data from that flight shows the
momentary onset of the stick shaker during the approach phase of
flight. The airplane subsequently landed without
incident. NTSB investigators have conducted interviews with
the pilots and check airman on board this flight and will continue
to investigate the incident.
Reports of airplane deviations resulting from distortion of
the instrument landing system (ILS) signal for runway 23 at
BUF. There is an existing Notice to Airmen (NOTAM) related to
this distortion condition. To date, investigation into these
reports has not revealed any connection to the accident flight.
Copyright Press release National Transportation Safety Board
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